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HomeMy WebLinkAboutPIT Test Data 10-19-2018Bradley Hoover HOBR1801-01 Project Address: Intersection of Hwys 19&20, NE PIT 1/TP10 Date:10/19/2018 Tester:Stephen Hanes Company:Northwestern Territories, Inc. Phone:360-452-8491 Email:stephen@nti4u.com Depth: 6.0 ft Bottom Width: 3 ft Bottom Length: 4 ft Bottom Area: 12 ft 2 Time Depth of Water (in.) 8:30 AM 1.0 9:30 AM 10.0 10:30 AM 10.5 11:30 AM 10.5 12:30 PM 10.5 1:30 PM 10.5 2:30 PM 10.0 Time Depth of Water (in.)Cumulative Vol.(ft3) Flow Rate (ft 3/hr)Infil. (in/hr) 2:30 PM 10.0 --- 2:45 PM 10.0 2.47 9.88 9.9 3:00 PM 10.0 1.76 7.04 7.0 3:15 PM 10.0 1.78 7.12 7.1 3:30 PM 10.0 1.76 7.04 7.0 Time Depth of Water (in.)Infil. (in/hr) 3:30 PM 10.0 - 3:45 PM 8.75 5.0 4:00 PM 7.5 5.0 4:15 PM 6.25 5.0 4:30 PM 5.0 5.0 Lowest steady-state infiltration rate:7.0 in/hr Correction Factors (2014 SMMWM, Table III-3.3.1) Site Variability:0.8 Test Method:0.5 Influent Control:0.9 Design Infiltration Rate:2.5 in/hr Small PIT test, within the footprint of the proposed drainage trench near the southwest corner of the property, approximately 100 ft north of the Uhaul property and 100 ft east of highway 20. After test, hole was excavated to 7.5' depth. No groundwater was encountered. Falling Head Period Steady-state Period Pre-soak Period Pilot Infiltration Test