HomeMy WebLinkAboutBLD2022-00505-04- Potable WaterRECEIVED BY DCD 8/30/2022
Spectra Labs - Kitsap, LLC (Poulsbo)
26276 Twelve Trees Ln NW Ste. C
Poulsbo, WA 98370
Phone: (360) 779-5141
www.spectra-lab.com
Sample No. Description Location Sampled
Spectra Labs - Kitsap, LLC (Poulsbo) received samples for David Spayth on Wednesday, August 3, 2022
at 2:20 pm. Unless otherwise noted, all samples were received in good condition and were tested in
accordance with the laboratory's quality control procedures. A summary of the samples received are
outlined below.
219646-01 Private 08/03/2022 11:50395 N Bay Way Port Ludlow
219646-02 Private 08/03/2022 11:50395 N Bay Way Port Ludlow
This report package contains laboratory sample results and any attachments listed below. If you have any
questions please call (360) 779-5141 or email us at www.spectra-lab.com.
08/09/2022 Page 1 of 1
This report is issued solely for the use of the person or company to whom it is addressed. Any use, copying or disclosure
other than by the intended recipient is unauthorized. If you have received this report in error, please notify the sender
immediately at 360-443-7845 and destroy this report promptly.
These results relate only to the items tested and the sample(s) as received by the laboratory. This report shall not be
reproduced except in full, without prior express written approval by Spectra Laboratories.
RECEIVED BY DCD 10/6/22
System ID No:
Date Received:8/3/2022
System Name:Private
Source Number(s):
Sample Purpose:Other
Date Reported:8/9/2022
County:Jefferson
System Group Type:Private
Send Report to:
David Spayth
20 Megs Way
Port Hadlock, WA 98339
Bill to:
David Spayth
20 Megs Way
Port Hadlock, WA 98339
IOC TEST PANEL
Complete or Selected Inorganics
Date Collected:
Sample Number:
8/3/2022
010-64602
Sample Location:395 N Bay Way Port Ludlow
Sample Composition:Single Source
Sample Type:Drinking Water
Sampler:
Sampler Phone No:
26276 Twelve Trees Ln NW Ste. C
Poulsbo, WA 98370
(360) 779-5141
TriggerSDRLDOH #MCL MethodAnalyteResultsUnitsExceeds
MCL
Analyst Analysis
Date
Qual.PQL
NV 8/6/2022EPA 300.02mg/L38.6Chloride0021 ---250---0.134
NV 8/4/2022EPA 300.00.5mg/LNDNitrate-N0020 ---10---0.0330
Include the original lab number, sample number, and collection date of original sample in either lab or sampler comments section.
(State Detection Reporting Limitl) The minimum reportable detection of an analyte as established by the department..
DOH drinking water response level. Systems with compounds detected at concentrations in excess of this level may be required to take
additional samples or monitor more frequently. Please contact your DOH drinking water regional office for further information.
(Maximum Contaminant Level) If the contaminant amount exceeds the MCL, please contact your regional DOH office to determine follow-up actions.
(Not Analyzed) In the results column, indicates this compound was not included in the current analysis.
(Not Detected) In the results column, indicates this compound was analyzed and not detected at a level greater than or equal to the SDRL.
The compound was not detected in the sample at or above the concentration indicated (usually the lab method reporting limit).
milligrams per liter or parts per million.
nephelometric turbidity units (a measure of water clarity).
Micro ohms per centimeter (a measure of the ability of the water to conduct electricity). One micro ohm per centimeter is equivalent to one micro
siemen per centimeter (uS/cm).
No existing trigger or MCL value.
Secondary MCL (Established for aesthetic purposes, not health based).
*Confirmation
SDRL:
Trigger Level:
MCL:
NA:
ND:
< (0.00x):
mg/L:
NTU:
mhos/cm:
--:
1:
NOTES:
Lab Qualifiers Comments:
Sample_Number:219646-02
Approved By
Angela Kaelin
Laboratory Manager
This report is issued solely for the use of the person or company to whom it is addressed. Any use, copying or disclosure other than by the intended recipient is
unauthorized. If you have received this report in error, please notify the sender immediately at 360-443-7845 and destroy this report promptly.
These results relate only to the items tested and the sample(s) as received by the laboratory. This report shall not be reproduced except in full, without prior express written
approval by Spectra Laboratories.
Page 1 of 1219646-02
RECEIVED BY DCD 10/6/22
RECEIVED BY DCD 10/6/22
RECEIVED BY DCD 10/6/22
1
106 N. Columbia Street
Wenatchee, WA 98801
(509)888-8081
August 19, 2022
Mr. David Spayth
25542 Rangewood Rd
Laguna Hills, CA 92653
Re: Review of Existing Seawater Intrusion Hydrogeologic Assessment
395 N Bay Way
Port Ludlow, WA
Project No. 22010
Dear David:
American Land and Water Consulting, LLC (American) has prepared this letter to present findings
and recommendations from our review of the Seawater Intrusion Hydrogeologic Assessment
completed by Aspect Consulting, LLC (Aspect) on behalf of previous owners of the property now
owned by David Spayth. Aspect previously submitted its report to Jefferson County to support
permitting of a single-family residence supplied by an existing well at 395 N. Bay Way (Parcel No.
976800063) in Jefferson County, Washington (Subject Property).
The findings and recommendations presented herein are based on our review of the following:
•Aspect’s Seawater Intrusion Hydrogeologic Assessment Report dated January 31, 2014
(Attachment 1) and an identical report dated August 1, 2006;
•Jefferson County Code (JCC) Chapter 18.22, Article III, Critical Aquifer Recharge Areas;
•Jefferson County Public Health (JCPH) Policy Statements 93-02 and 96-02;
•Washington Department of Ecology’s (Ecology) Online Well Log Database (Ecology, 2022);
•Regional surficial geologic maps (DNR, 2022) and hydrogeologic reports (Jones et al., 2011);
and
•Historical aerial imagery of the Subject Property and vicinity.
Our review did not include a site visit or confirmation that well construction and siting requirements
have been met under WAC 173-160 (Minimum Standards for Construction and Maintenance of
Wells).
Background
Jefferson County has determined that the existing well at the Subject Property (Snider Well, Ecology
ID AHL-983) is located within a High-Risk Seawater Intrusion Protection Zone (SIPZ) under the
County’s Critical Areas Code, Critical Aquifer Recharge Areas (JCC Chapter 18.22, Article III) because
it lies within 1,000 feet of a well (Hanauer Well, No Ecology ID, Well Report ID 45198) having
chloride concentrations exceeding 200 milligrams per liter (mg/L).
For existing wells meeting requirements of WAC 173-160 (i.e. when no variance is required), JCC
18.22.330(8) requires the applicant to provide a hydrogeologic evaluation of potential impacts from
using wells to supply new development within a High Risk SIPZ. The hydrogeologic evaluation must
satisfy requirements of JCC 18.22.930(2)(b). It also must demonstrate that proposed use of the well
RECEIVED BY DCD 8/30/2022
2
106 N. Columbia Street
Wenatchee, WA 98801
(509) 888-8081
will not cause impairment of existing water rights including permit exempt wells and will not be
detrimental to the public interest including degradation of aquifer water quality resulting from
pumping-induced seawater intrusion. The report documenting a hydrogeologic evaluation is
required to be transmitted to JCHD and Ecology for review.
Aspect initially submitted a hydrogeologic report, dated August 1, 2006, to Jefferson County on
behalf of a previous property owner, Ms. Maggie Lang. This report was entered into the County’s
records for the Subject Property. Aspect completed a second report, dated January 31, 2014, on
behalf of a subsequent property owner, Ms. Evelyn Dickinson (Attachment 1). These two reports
are identical expect for the dates. We could not determine whether the 2014 report was accepted
by the County into the record for the Subject Property, or if either report was reviewed by JCHD and
Ecology.
We understand that a water system consisting of a submersible well pump, flow meter, flow
restrictor, and 3,000-gallon storage tank was installed at the Subject Property by a previous owner
consistent with recommendations in Aspect’s report.
The current owner of the Subject Property, Mr. David Spayth, intends to use the well and water
system to supply domestic water for a proposed single-family residence.
Summary of the Existing Report
Aspect’s report documents findings and recommendations of its hydrogeologic assessment of
potential impacts from using Well AHL-983 for domestic use.
Aspect’s hydrogeologic assessment consisted of a review of applicable regulations and readily
available geologic and hydrologic information and well logs completed in the vicinity of the Subject
Property and completion of a low-discharge, step-rate pumping test, and water quality analysis.
Aspect conducted the pumping test on May 23, 2006 at discharge rates of 1, 2, and 3 gallons per
minute (gpm) over a period lasting approximately 6 hours. Groundwater levels in the pumping well
were monitored throughout the test. Water quality monitoring throughout the test consisted of
using Hatch test strips to measure chloride concentrations and a meter to measure Specific
Conductivity. Water quality samples were collected at the end of each step rate and submitted for
laboratory analysis for the aforementioned parameters. Water level drawdown and recovery curves
were plotted next to water quality parameters for each discharge step rate to quantify hydraulic
properties of the well and aquifer and to analyze impacts of pumping on water quality i.e. seawater
intrusion.
Conclusions and recommendations for Well AHL-983 from Aspect’s report:
• The was drilled to a total depth of 205 feet below ground surface (bgs) and is completed in a
water bearing zone of fractured basalt bedrock between 118 and 205 feet bgs, or about 0 to
87 feet below sea level based on ground surface elevation of the wellhead obtained using a
GPS;
• Static water level in the well was measured at about 83 feet below the top of casing, or
about 34 feet above sea level. The well does not appear to be tidally influenced based on
relatively constant baseline water levels observed prior to the start of the pumping test;
RECEIVED BY DCD 8/30/2022
3
106 N. Columbia Street
Wenatchee, WA 98801
(509) 888-8081
• The completion zone within the aquifer is confined. Confining units are likely comprised of
massive, unfractured layers of basalt and an overlying layer of clay and gravel;
• Groundwater flow is generally northeasterly from an upland recharge region toward Puget
Sound.
• Numerous wells in the vicinity of the Subject property are also completed in the basalt
aquifer; however, few nearby domestic wells are likely pumping from the same fracture
zone due to probable lateral discontinuity of the fractures.
• The well is low yield. Total drawdown after 6 hours of pumping was about 16 feet resulting
in estimates for specific capacity at the well between 0.34 and 0.36 gpm per foot of
drawdown;
• Estimates of aquifer transmissivity based on drawdown analysis range between 210 and 695
gallons per day (gpd) per foot (gpd/ft) with a geometric mean of approximately 390 gpd/ft
(52 ft2/day);
• A pumping rate up to 3 gpm was determined to have minimal impact on physical water
availability in the aquifer and will not impair existing wells based on a maximum lateral
boundary of pumping influence estimated at 99 feet from Well AHL-983. There appears to
be no wells within 100 feet of the Well AHL-983;
• Chloride concentrations remained stable at background levels (about 40 mg/L) using a
pumping at a rate of 1 gpm but became elevated when pumping rates were increased to 2
to 3 gpm; and
• A pumping rate of 1 gpm and 400 gpd was recommended to prevent an increase in chloride
concentrations observed during the pumping test.
Conclusions and Recommendations from Our Review of the Existing Report
The following conclusions and recommendations are based on our review of Aspect’s report and
other relevant information described in this report:
• Aspect’s report appears to meet applicable requirements under JCC 18.22.930(2)(b) and its
conclusions are consistent with other hydrogeologic reporting for the area (e.g. Jones et al.,
2011);
• We concur with the conclusions and recommendations presented by Aspect including
maintaining a flow rate of 1 gpm and 400 gpd to provide reasonable assurance that
pumping from Well AHL-983 for domestic use will not impair nearby wells or induce
seawater intrusion in the aquifer;
• Key considerations that we used to reach the above conclusion include:
o We identified no evidence that conditions have changed at the Subject Property or
its vicinity since Aspect completed its hydrogeologic evaluation in 2006 that would
change the conclusions and recommendations presented by Aspect;
RECEIVED BY DCD 8/30/2022
4
106 N. Columbia Street
Wenatchee, WA 98801
(509) 888-8081
o Aspect observed that a pumping rate of 1 gpm resulted in stable chloride
concentrations of about 40 mg/L over, which is within the range for fresh
groundwater and background conditions;
o A grab sample collected from Well AHL-983 by Mr. Spayth on August 3, 2022 was
analyzed for chloride by Sprectra Laboratories of Poulsbo, Washington. Results
indicate a chloride concentration of 38.6 mg/L, which is consistent with background
chloride concentrations observed during Aspect’s 2006 pumping test; and
o The recommended daily withdrawal rate of 400 gallons is within the daily flux of
groundwater flowing northeasterly through the aquifer based on estimate aquifer
transmissivity of 390 gpd/ft. The recommended daily withdrawal rate is not
expected to be sufficient to reverse the natural groundwater gradient over the long-
term;
• According to Washington Department of Health’s (DOH) Water System Design Manual
(DOH, 2019), average daily demand (ADD) for indoor use by a single-family residence if 200
gpd. DOH also recommends planning for a maximum daily demand (MDD) of 1.5 x ADD, or
350 gpd for indoor use. Combined with the existing 3,000-gallon storage tank installed for
the water system, the recommended daily withdrawal rate of 400 gallons will be sufficient
to meet indoor ADD with a nominal quantity of water available for outdoor use and will be
capable of meeting MDD for indoor use; and
• We could not verify whether JCHD and Ecology have reviewed Aspect’s report as required
under JCC 18.22.330(8). If these reviews were not completed, we recommend the agencies
review Aspect’s report in combination with this letter.
References
Jones, J.L., Welch, W.B., Frans, L.M., and Olsen, T.D., 2011, Hydrogeologic framework, groundwater
movement, and water budget in the Chimacum Creek basin and vicinity, Jefferson County,
Washington: U.S. Geological Survey Scientific Investigations Report 2011–5129
Washington Department of Ecology (Ecology), 2022, Washington State Well Report Viewer
interactive map, online at
https://appswr.ecology.wa.gov/wellconstruction/map/WCLSWebMap/default.aspx
Washington State Department of Health, 2019, Water System Design Manual, Washington State
Department of Health Office of Drinking Water, Olympia, Washington.
Washington Department of Natural Resources (DNR) Division of Geology and Earth Resources,
2022, Washington Interactive Geologic Map, online at http://www.dnr.wa.gov/geologyportal.
Limitations
Work for this project was performed for David Spayth (Client) and this report was prepared
consistent with recognized standards of professionals in the same locality and involving similar
conditions, at the time the work was performed. No other warranty, expressed or implied, is made
RECEIVED BY DCD 8/30/2022
5
106 N. Columbia Street
Wenatchee, WA 98801
(509) 888-8081
by American Land and Water Consulting, LLC. The information above is for preliminary, planning-
level design and should not be used for final design or construction.
We appreciate the opportunity to work with you. If you have any questions, please contact Bill
Sullivan at (509) 699-0682 or Bill@AmericanLW.com.
Sincerely,
Bill Sullivan, LHG, CWRE (No. 008)
Principal Hydrogeologist
Bill@AmericanLW.com
(509) 699-0682
Attachments:
1. Seawater Intrusion Hydrogeologic Assessment, Aspect Consulting, January 31, 2014
RECEIVED BY DCD 8/30/2022
Attachment 1
RECEIVED BY DCD 8/30/2022
earth +water Aspect Consulting, LLC 350 Madison Avenue N. Bainbridge Island, WA 98110 206.780.9370 www.aspectconsulting.com
January 31, 2014
Evelyn Dickinson
1812 19th Avenue, Apt. 307
Seattle, Washington 98122-7518
Re: Seawater Intrusion Hydrogeologic Assessment
Project No. 060115-001-01
Dear Mrs. Dickinson:
This letter-report presents a hydrogeologic assessment of a domestic water supply well (Snider
well) located at 395 North Bay Way, near Port Hadlock, Washington. It is our understanding
that the domestic water supply well is located within a 1,000-foot radius of a well designated
as a High Risk Seawater Intrusion Protection Zone (SIPZ), as classified by Jefferson County.
The Jefferson County Department of Community Development requires that a hydrogeologic
assessment be submitted as part of the building permit application process for proof of potable
water due to the location of the well within the High Risk SIPZ.
In preparing this hydrogeologic assessment, we have conducted a low discharge pump test,
performed water quality sampling and reviewed the following material on which we base our
findings and conclusions:
Water Well Reports on file with the Washington Department of Ecology (Ecology) and the
Jefferson County Well Database.
On-site low discharge pump test data.
On-site well water quality data, including both chloride levels and specific conductivity.
Jefferson County Unified Development Code.
Property Location Maps, Topographic Maps.
Jefferson County Coastal Seawater Intrusion Policy and Ordinance.
Geologic Map of Eastern Jefferson County.
WRIA 17 report on Groundwater Quality Data Summary for Water Resources Inventory
Area 17.
Ecology Water Right Application Tracking System (WRATS) database.
Project Description
The Snider well is located on a partially developed property near Puget Sound, approximately
5 miles south of Port Hadlock, Washington. Figure 1 is a site location and parcel map that
shows the layout of the Snider property (Parcel Number: 976800063) relative to surrounding
parcels. Review of Figure 1, derived from the United States Geological Survey 1:24000 Port
Ludlow topographic map, indicates that the Snider well is approximately 625 feet (ft) from the
shoreline at an approximate elevation of 118 ft above mean sea level (MSL). The location of
the Snider well was obtained with a Global Positioning System (GPS) unit on May 23, 2006.
RECEIVED BY DCD 8/30/2022
Mrs. Evelyn
Dickinson
January 31, 2014
Project No. 060115-001-01
Initial water quality testing of the Snider well indicated a chloride concentration of 31.1
milligrams per liter (mg/l) on July 25, 2004 and 69.6 mg/l on April 25, 2006.
Jefferson County has established a High Risk SIPZ in the vicinity of the Lee Hanauer
properties (Parcel Numbers: 921292003 and 921292004). A High Risk SIPZ extends in a
1,000-foot radius from any individual well that exhibits a chloride reading of 200 mg/l or
greater. The Snider well lies within the established High Risk SIPZ and therefore requires the
development of a hydrogeologic assessment per the Jefferson County Unified Development
Code.
Hydrogeologic Assessment
Well Log Information
Water Well Reports on file with Ecology were obtained and reviewed for wells which are
completed in the same section as the Snider well (T29N/R01E-29). A summary of well
completion data contained in the well reports is presented in Table 1. Well reports for the
Snider and Hanauer wells are provided in Attachment 1.
The Snider water supply well was installed on July 7, 2004 by Mel Williams Drilling of
Sequim, Washington. The 6-inch-diameter well was completed to a depth of 205 ft below
ground surface (bgs), with a 4.5-inch-diameter PVC liner extending from 8 ft bgs to the bottom
of the well. The well has a casing stick-up of 1.07 ft, measured from the ground surface to the
top of casing, and the pump was set at approximately 120 ft below the top of casing (btoc),
according to personnel from Bayview Pumps.
The Snider well produces water primarily from a basalt aquifer between 118 and 205 ft bgs
(between 0 and -87 ft MSL). It is assumed the water-bearing zones of the basalt aquifer are
associated with fractures within the basalt. These water-bearing zones are likely confined by
zones of massive, unfractured basalt. A brown, clay, and gravel layer listed on the well report
from 0 to 34 ft bgs also likely provides additional confinement of the basalt aquifer. A static
water level of 83 ft btoc (33.93 ft MSL) was recorded for the well on July 7, 2004. An initial
2-hour pump test performed by Bayview Pumps at a rate of 5 gallons per minute (gpm)
produced approximately 30 ft of drawdown in the well. These results indicate the well is not
highly productive and has a specific capacity of 0.17 gpm/ft.
Based on a geologic map of eastern Jefferson County published on the Jefferson County
website (http://www.co.jefferson.wa.us/idms/pdfs/geo_ec.pdf), the most prominent geologic
unit exposed at the surface in the vicinity of the Snider well is Vashon Lodgement Till (Vlt).
In addition, an older Mudstone, Siltstone and Shale unit (Ts) can be found along the shoreline
of Oak Bay near the Snider well. Based on the materials described in the Snider well report,
the well is likely completed in Tertiary Basalt (Tb). Table 1 indicates that numerous wells in
the vicinity of the Snider well are completed in Tertiary Basalt with specific capacities ranging
between 0.01 and 0.39 gpm/ft.
The Ecology well report database lists two wells owned by Chip and Lee Hanauer (Parcel
Numbers: 921292003 and 921292004) in the vicinity of the Snider property which likely
resulted in the High Risk SIPZ designation by Jefferson County. The first well is listed as
being owned by Chip Hanauer and was completed at a depth of 176 ft bgs on June 4, 1993.
Page 2
RECEIVED BY DCD 8/30/2022
Mrs. Evelyn
Dickinson
January 31, 2014
Project No. 060115-001-01
The well is perforated from 56 to 176 ft bgs and produces water from sequences of grayish-
green basalt and gray shale. Water quality testing of the well after installation indicated
chloride concentrations ranging between 250 and 400 mg/l. The second well is listed as being
owned by Lee Hanauer and was dug to a depth of 14.8 ft bgs. The well report indicates that
the well was abandoned on July 25, 2003. These well reports are provided in Attachment 1.
Lateral continuity of the water-bearing basalt zones in the vicinity of the Snider well is
unknown; however, it is assumed that the fractures are relatively discontinuous. Therefore, it
is likely that relatively few of the domestic water supply wells in the vicinity of the Snider well
are producing water from the same fractured basalt zone.
Groundwater Elevation
Groundwater flows from areas of high head (elevation) to areas of low head. Based on
topography, groundwater in the vicinity of the Snider well is assumed to be flowing in a
northeasterly direction and discharging into Puget Sound. Static groundwater level data
collected at the time of well completion indicated a groundwater level of 83 ft btoc (33.93 ft
MSL). A static groundwater level of 81.89 ft btoc (35.04 ft MSL) was measured prior to the
pump test on May 23, 2006. These measurements indicate a relatively stable depth to water in
the vicinity of the Snider well. In addition, baseline groundwater level measurements recorded
prior to the pump test also indicated a relatively stable groundwater level, thus indicating that
the well is not tidally influenced. Based on the static water level data, approximately 37 to 38
ft of groundwater drawdown is currently available within the well.
Low Discharge Pump Test Data
A low discharge pump test was conducted at the Snider well on May 23, 2006 by Aspect
Consulting, LLC. The existing well pump was used to conduct the test and Bayview Pumps
was contracted to install a temporary flowmeter to measure the pumping rate during the test
and ensure that the electrical generator system powering the pump was functioning properly.
A low discharge flow rate of 3 gpm or less was identified as a pumping rate which would have
minimal impact on the aquifer and is in accordance with the voluntary requirements of water
conservation measures recommended by Jefferson County for wells completed in SIPZ’s. The
well was pumped at variable flow rates (steps) of 1.0 gpm, 2.0 gpm, and 3.0 gpm for a total
pumping period of 371 minutes (approximately 6 hours). Groundwater level drawdown
measurements, discharge measurements, and conductivity measurements were recorded
throughout the test. In addition, Hach test strips were used to measure chloride concentrations
during the test. Water quality samples were collected at the end of each pumping period and
submitted for laboratory analysis (see further description on water quality results below).
Attachment 2 contains water level, pump rate, and water quality parameters measured during
the pump test. A graphical plot of the pump test data showing drawdown at different pumping
rates as well as conductivity readings and chloride concentrations for the duration of the test is
shown on Figure 2.
As Figure 2 demonstrates, baseline groundwater level data was relatively constant prior to the
start of the pump test. Therefore, it is assumed that the Snider well is not tidally influenced
and no corrections of the pump test data are required to account for tidal influences. Based on
Figure 2, a total drawdown of 15.9 ft was observed during the entirety of the pump test and the
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RECEIVED BY DCD 8/30/2022
Mrs. Evelyn
Dickinson
January 31, 2014
Project No. 060115-001-01
following groundwater level drawdowns and respective specific capacities were observed for
each of the variable pumping rates:
Pumping
Rate
(gpm)
Drawdown
(ft)
Specific
Capacity
(gpm/ft)
1.0 2.9 0.34
2.0 4.7 0.43
3.0 8.3 0.36
Low Discharge Pump Test Analyses
Transmissivity is the quantitative measure of an aquifer’s ability to transmit water and can be
determined for various pumping rates of the low discharge pump test based on the Cooper-
Jacob Straight-Line Method (Driscoll, 1986):
T = 264Q/Δs’
Where: T = Transmissivity (gpd/ft)
Q = Discharge (gpm)
Δs’ = Change in residual drawdown over one log cycle (ft)
Figures 3, 4, and 5 present the transmissivity calculations for the various flow rates of the
pump test conducted on May 23, 2006. The transmissivity of the Snider well basalt aquifer
was determined to range between 210 and 695 gpd/ft with a geometric mean of approximately
390 gpd/ft. The transmissivity calculations indicate that the basalt aquifer tapped by the Snider
well is not highly productive, but should be capable of sustaining a 3.0 gpm pumping rate with
only a moderate amount of drawdown.
Based on information obtained during well testing, a distance to the seaward or downgradient
stagnation point (area in the groundwater flow field at which groundwater is not moving
towards the well) can be calculated from the following equation (EPA, 1993):
Kbi
QXLπ2−=
Where: XL = Downgradient distance to stagnation point (ft)
Q = Pumping rate (ft3/sec)
K = Hydraulic conductivity (ft/sec) = Transmissivity / Aquifer thickness
b = Aquifer thickness (ft)
i = Groundwater gradient (unitless) = Groundwater height above sea level /
distance to shoreline from well.
Likewise, the lateral boundary of the pumping influence of the Snider well (or lateral extent at
which groundwater enters the well) can be estimated by the following equation (EPA, 1993):
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RECEIVED BY DCD 8/30/2022
Mrs. Evelyn
Dickinson
January 31, 2014
Project No. 060115-001-01
Kbi
QYL2±=
Where: YL = Lateral boundary (ft)
The results of these analyses, assuming an aquifer transmissivity of 390 gpd/ft, an aquifer
thickness of 87 ft and a groundwater gradient of 0.056 are summarized in the following table:
Rate
(gpm) XL (ft) YL (ft)
3 31.4 98.7
2 20.9 65.8
1 10.5 32.9
This analysis suggests that pumping the Snider well at a rate of 3.0 gpm will withdraw
groundwater at a distance of approximately 99 ft from the well on the downgradient or seaward
side and at a 31-foot lateral distance. According to the GPS well location and parcel map
(Figure 1), this analysis suggests that at a pumping rate of 3.0 gpm, the area of groundwater
contributing to the well is contained within the Snider parcel and should not interfere or impair
nearby existing wells. Based on available water well reports and water right certificates (Table
1), there appears to be no domestic water supply wells within the area of contribution that
would be affected by withdrawals from the Snider well under low (3 gpm or less) pumping
rates.
Water Quality Data
Seawater intrusion can be evaluated by collecting water quality data at a well and performing
measurements of chloride concentrations. Groundwater aquifers in direct hydraulic continuity
to the sea will typically contain both freshwater and seawater. Freshwater, which has a lower
density than seawater, will float on top of the denser seawater. A mixing zone between the
freshwater and seawater occurs as a result of hydrodynamic dispersion. This mixing zone
typically separates natural background freshwater (chloride levels typically <50 parts per
million [ppm] or milligrams per liter [mg/l]) from seawater (chloride levels on the order of
19,000 mg/l) (Pacific Groundwater Group & Parametrix, 2000). Jefferson County has defined
the following three categories of SIPZ’s:
Coastal SIPZ – All islands and land area within ¼-mile of marine shorelines and
associated aquifers;
At Risk SIPZ – Areas within 1,000 feet of a groundwater source with a history of chloride
analyses between 100 mg/l and 200 mg/l;
High Risk SIPZ – Areas within 1,000 feet of a groundwater source with a history of
chloride analyses over 200 mg/l.
Chloride concentrations and specific conductivity data were collected in the field during the
pump test on May 23, 2006 and from groundwater samples which were also collected during
the pump test and submitted for laboratory analysis. Specific conductivity is a measure of the
ability of water to conduct electricity and is measured in units of micro-Siemens per centimeter
(µS/cm). Specific conductivity can be easily measured with field monitoring equipment and
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RECEIVED BY DCD 8/30/2022
Mrs. Evelyn
Dickinson
January 31, 2014
Project No. 060115-001-01
provides a good field tool for evaluating the relative level of dissolved compounds, such as
chloride, in groundwater.
The data (Figure 2) show that initially water from the Snider well had a specific conductivity
of 880 µS/cm, which can likely be attributed to the long period of time since the well had been
previously pumped. As pumping progressed at a rate of 1.0 gpm, specific conductivity values
decreased to approximately 420 µS/cm before slowly increasing to approximately 480 µS/cm
and remaining relatively constant during the remainder of the 1.0 gpm step. At a pumping rate
of 2.0 gpm, specific conductivity values slowly increased from 480 µS/cm to approximately
700 µS/cm. Although the rate at which specific conductivity values increased during the 2.0
gpm step decreased slightly as the test progressed, specific conductivity values did not stabilize
at the end of the 2.0 gpm step as observed at the end of the 1.0 gpm step. At a pumping rate of
3.0 gpm specific conductivity values increased at a fairly linear rate from 700 µS/cm to
approximately 880 µS/cm.
Chloride concentrations also displayed a similar trend to specific conductivity measurements.
Chloride concentrations were measured during the pump test using Hach test strips and were
found to range from less than 28 mg/l to approximately 200 mg/l. At the end of the 1.0 gpm
step, chloride concentrations remained relatively stable at approximately 40 mg/l. However,
chloride concentrations increased to approximately 120 mg/l at the end of the 2.0 gpm step and
to approximately 200 mg/l at the end of the 3.0 gpm step.
Groundwater samples were collected on May 23, 2006 at the end of each step of the low
discharge pump test and submitted to Twiss Analytical for analysis. A total of 736 gallons of
water was pumped from the Snider well during the test. Chloride and specific conductivity
levels analyzed by Twiss Analytical are summarized in the following table.
Discharge Rate
(gallons per
minute, gpm)
Elapsed Time
(minutes) Sample Date
Specific
Conductivity
(µS/cm)
Chloride
(mg/l)
1.0 110 5/23/06 478 39.2
2.0 229 5/23/06 697 119
3.0 367 5/23/06 887 191
All water quality samples collected for this investigation were analyzed by Twiss Analytical, a
Washington state certified laboratory located in Poulsbo, Washington. The water quality
reports are presented in Attachment 3. The results of the laboratory analyses are consistent
with the chloride concentrations and specific conductivity values measured in the field (Figure
2).
Results from the water quality analyses indicate that chloride concentrations of groundwater
from the Snider well are below the United States Environmental Protection Agency Secondary
Maximum Contaminant Level (SMCL) of 250 mg/l and are relatively stable when the well is
pumped at a rate of 1.0 gpm. However, pumping the Snider well at rates of 2.0 and 3.0 gpm
results in an increase of chloride concentrations to 119 and 191 mg/l, respectively. Therefore,
it is recommend that the Snider well be pumped at a rate of not more than 1.0 gpm in order to
prevent an increase in chloride concentrations similar to that observed during the step test
Page 6
RECEIVED BY DCD 8/30/2022
Mrs. Evelyn
Dickinson
January 31, 2014
Project No. 060115-001-01
performed on May 23, 2006. Pumping at a rate of 2.0 gpm would be feasible, but would likely
result in an overall increase in the chloride concentration of groundwater from the Snider Well.
Unified Development Code Requirements
The following table lists mandatory requirements associated with High Risk SIPZ’s as well as
specific requirements for all development proposals within 0.25 miles of any marine shoreline.
Jefferson County
Unified
Development Code
(UDC)
Requirement
Description UDC Section Reference
Stormwater Disposal All new developments within 0.25 miles of any
marine shoreline are required to infiltrate all
stormwater onsite to help prevent seawater from
intruding landward into aquifers.
Chapter 18.15 – Land Use
Districts 18.15.255 Protection
Standards, Article VI-E Critical
Aquifer Recharge Areas (2)(a)
Stormwater Disposal
High Risk SIPZ Mandatory Actions
1)Water conservation measures (See
Attachment 4)
2)Submittal of chloride concentration with
building permit application
3)Installation of a source-totalizing meter (flow)
4)On-going well monitoring for chloride
concentration
5)Submittal of data to county
Chapter 18.15 – Land Use
Districts 18.15.255 Protection
Standards, Article VI-E Critical
Aquifer Recharge Areas, (9) Well
Drilling, Land Division, and
Building Permits in Seawater
Intrusion Protection Zones, (d)(iii)
High Risk SIPZ
Conclusions
The following conclusions are developed based on a review of the available hydrogeologic
data:
1.The Snider well is completed at a depth of 205 ft bgs in a confined, water-bearing basalt
aquifer which does not appear to be tidally influenced.
2.The pump test data indicates that the Snider well is capable of sustaining a pumping rate of
3.0 gpm with a moderate amount of drawdown. At 3.0 gpm, the downgradient radius of
influence would not extend to the sea and the lateral boundary of influence would not
affect existing wells in the area. Pumping should not exceed a discharge of 3.0 gpm and
only 400 gallons per day or less should be pumped as recommended in the attached Water
Conservation Measure list developed by the county (Attachment 4). If more than 400
gallons per day of water usage is expected, it is advised that a water system design
incorporating a storage tank system is considered.
3.Although the Snider well is capable of sustaining a pumping rate of 3.0 gpm, it is
recommended based on water quality analyses that the well be pumped at no more than 1.0
Page 7
RECEIVED BY DCD 8/30/2022
Mrs. Evelyn
Dickinson
January 31, 2014
Project No. 060115-001-01
gpm. Pumping at a rate of 1.0 gpm would prevent a likely increase in chloride
concentrations associated with higher pumping rates (2.0 and 3.0 gpm) as observed during
the step test performed on May 23, 2006.
4.The High Risk SIPZ designation requires:
a.The use of water conservation measures outlined in Attachment 4.
b.Submittal of chloride concentration with building permit application.
c.Installation of totalizing flow meter to record the volume of water pumped from the
well.
d.On-going well monitoring for chloride concentration.
e.Submittal of flow and chloride data to the county per monitoring program.
5.All stormwater is required to be infiltrated on-site. It is recommended that the infiltration
should be directed in an area between the well and the sea, which will further protect the
aquifer from seawater intrusion.
Based on the data available for review, it appears that there is reasonable assurance that
pumping the Snider well under low discharge rates will not cause impairment to existing wells
in the surrounding area. Implementation of water conservation measures and stormwater
infiltration will provide additional measures of protection in the prevention of the further
advancement of seawater intrusion.
References
Driscoll, F.G., 1986, Groundwater and Wells (2nd Edition), St. Paul, Minnesota, Johnson
Screens, p. 252 – 257.
Environmental Protection Agency, February 1993, Wellhead Protection: A Guide for Small
Communities, EPA/625/R-93/002.
Jefferson County Ordinance No. 06-0609-03, June 9, 2003.
Jefferson County Unified Development Code, Chapter 18.15, Land Use Districts.
Jefferson County Web Page, Geology Map; Eastern Jefferson County,
http://www.co.jefferson.wa.us/idms/pdfs/geo_ec.pdf, 2/21/95.
Pacific Groundwater Group and Parametrix, Inc., June 2000, Groundwater Quality Data
Summary for Water Resources Inventory Area 17, prepared for Water Resources
Inventory Area 17 Planning Unit.
Page 8
RECEIVED BY DCD 8/30/2022
RECEIVED BY DCD 8/30/2022
W :\060115 S nider W ell\U pdated 2014 R eport\W ell R ecords
Table 1 - Well Records
Vicinity of Snider Well (T29N/R1E-29)
Snider Pump Test
Port Hadlock, WA
Page 1 of 2
Town
N
Range
E Section Qtr
Section
Qtr-Qtr
Section Original Owner
Jefferson
County Parcel
Number
Proposed
Use
Drilled
Depth (ft)
Completed
Depth (ft)
Diameter
(in)
Open
From (ft)
Open
To (ft)
Static Water
Level (ft
TOC)
Yield
(gal/min)
Drawdown
(ft)
Specific
Capacity
(gpm/ft)
Completion
Date Producing Unit Document
Number Date Source Quantitiy
(gpm)Data Source
29 1 29 --ANN WILBERT -Domestic 118 118 6 30 118 41 1 75 0.013 8/25/1987 Basalt ----Ecology & Jefferson
Co
29 1 29 --JAMES OTT -Domestic 105 105 6 17 105 29.5 4 --9/1/1993 Basalt ----Ecology
29 1 29 --JIM GEORHEARD -Domestic 57 57 6 38 2 --7/3/1984 Basalt ----Ecology & Jefferson
Co
29 1 29 --LOUIS STORKEN -Domestic 245 245 6 --50 5 185 0.027 3/20/1981 Basalt ----Ecology & Jefferson
Co
29 1 29 --MELVIN SANDEN -Domestic 130 130 6 --31 7 92 0.076 8/18/1978 Sandstone &
Basalt ----Ecology & Jefferson
Co
29 1 29 --OAK BAY ASS. N.-Municipal 200 164 6 95 160 60 1.5 36.5 0.041 5/7/1982 Sandstone,
Shale & Basalt ----Ecology & Jefferson
Co
29 1 29 --SYLVIA REVELLE 976800014 Domestic 108 108 6 88 108 45 15 55 0.273 9/2/1987 Basalt ----Ecology & Jefferson
Co
29 1 29 --TOM PAULSON -Domestic 105 105 6 85 105 59 6 38 0.158 11/14/1988 Shale & Basalt ----Ecology & Jefferson
Co
29 1 29 --TOM PAULSON 976800011 Domestic 108 108 6 88 108 59 12 50 0.240 8/1/1991 Basalt ----Ecology & Jefferson
Co
29 1 29 --TONY GODENHEIMER -Domestic 162 162 6 ---50 --5/17/1991 Sandstone &
Basalt ----Ecology
29 1 29 --TRUDY BOLITKER 976800073 Domestic 150 150 6 --21 50 129 0.388 7/14/1986 Sandstone &
Basalt ----Ecology & Jefferson
Co
29 1 29 E SE STORKEN 921294005 Domestic 56 56 6 --18 ---10/4/1999 ----Jefferson Co
29 1 29 NE SE JIM CLAWSON -Domestic 100 100 6 50 4 46 0.087 12/31/1991 Sandstone ----Ecology
29 1 29 NE SW MRS. BOB WILLIAMS -Domestic 99 101 6 79 99 33 5 52 0.096 11/14/1988 Conglomerate &
Sandstone ----Ecology & Jefferson
Co
29 1 29 NW NW CHIP HANAVER -Domestic 176 176 6 56 176 19.25 2.5 --6/4/1993 Shale & Basalt ----Ecology
29 1 29 NW NW DICK CLOUDY -Domestic 105 105 6 65 105 55 1 48 0.021 8/12/1993 Shale ----Ecology
29 1 29 NW NW DICK CLOUDY -Domestic 59 59 6 45 59 20 10 34 0.294 8/15/1993 Sandstone ----Ecology
29 1 29 NW NW GENE HANSON -Domestic 114 114 6 94 114 45 3 63 0.048 12/28/1993 Sandstone ----Ecology
29 1 29 NW NW GEORGE DEERING 921292016 Domestic 196 196 6 178 196 54 6 180 0.033 4/1/1994 Sandstone ----Ecology & Jefferson
Co
29 1 29 NW NW HAROLD GITT -Domestic 87 87 6 --32 5 --10/16/1985 Sandstone &
Basalt ----Ecology & Jefferson
Co
29 1 29 NW NW HAROLD GITT -Domestic 33 120 6 80 120 37 20 65 0.308 8/9/1993 Sandstone ----Ecology
29 1 29 NW NW JOHN ASANARA -Domestic 39 39 6 34 39 10 15 10 1.500 7/15/1972 Gravel & Sand ----Ecology & Jefferson
Co
29 1 29 NW NW OAK BAY HOME
OWNERS ASSOC 921292035 Municipal 82 82 6 62 82 55 2.5 20 0.125 12/15/2005 Sandstone ----Ecology
29 1 29 NW NW OAK BAY WATER -Municipal 160 160 6 140 160 44 1 114 0.009 8/8/1992 Basalt ----Ecology
29 1 29 NW NW OAK BAY WATER -Municipal 28 28 6 14 18 9 12 9 1.333 8/10/1992 Clay, Sand &
Gravel ----Ecology
29 1 29 NW NW OAK BAY WATER -Municipal 90 90 6 50 90 40 2 53 0.038 8/13/1992 Sandstone ----Ecology
29 1 29 NW NW RICHARD GITT 921292055 Domestic 83 83 6 45 83 25 5 50 0.100 12/14/1994 Sandstone ----Ecology & Jefferson
Co
29 1 29 NW NW RICK GITT 921292053 Domestic 160 142 6 54 0.75 140 0.005 10/24/2000 Clay, Sandstone
& Basalt ----Ecology & Jefferson
Co
Location ID Well Information Well Productivity Water Rights
RECEIVED BY DCD 8/30/2022
W :\060115 S nider W ell\U pdated 2014 R eport\W ell R ecords
Table 1 - Well Records
Vicinity of Snider Well (T29N/R1E-29)
Snider Pump Test
Port Hadlock, WA
Page 2 of 2
Town
N
Range
E Section Qtr
Section
Qtr-Qtr
Section Original Owner
Jefferson
County Parcel
Number
Proposed
Use
Drilled
Depth (ft)
Completed
Depth (ft)
Diameter
(in)
Open
From (ft)
Open
To (ft)
Static Water
Level (ft
TOC)
Yield
(gal/min)
Drawdown
(ft)
Specific
Capacity
(gpm/ft)
Completion
Date Producing Unit Document
Number Date Source Quantitiy
(gpm)Data Source
Location ID Well Information Well Productivity Water Rights
29 1 29 NW SE JIM LEVERETT 976800003 Domestic 124 100 6 30 100 29.8 2.5 50 0.050 7/26/1996 Sandstone ----Ecology & Jefferson
Co
29 1 29 NW SE LEE HANAUER 921292004 Domestic 14.83 14.83 72 ------7/25/2003 Abandoned ----Ecology
29 1 29 NW SW JEFF PETERS -Domestic 58 58 6 --8 5 60 0.083 9/30/1992 Sandstone ----Ecology
29 1 29 NW SW JEFF PETERS 921292069 Domestic 234 234 6 214 234 164 7 60 0.117 12/22/1997 Shale ----Ecology & Jefferson
Co
29 1 29 NW SW KELLY SNIDER 976800063 Domestic 205 205 6 --83 4 --7/7/2004 Sandstone &
Basalt ----Ecology
29 1 29 SE NW JEFF PETERS 976800053 Domestic 204 204 6 --56 12 --12/23/2003 Basalt ----Ecology
29 1 29 SE SE AYLA HIGGINS 921294008 Domestic 224 224 6 --26 25 --12/6/2004 Basalt ----Ecology
29 1 29 SE SE DONN ALEXANANDER 921294009 Domestic 164 164 6 56 144 20 6 135 0.044 8/22/1988 Shale & Basalt ----Ecology & Jefferson
Co
29 1 29 SE SE IRENE STORKEN -Domestic 63 63 6 16 61 18 ---10/6/1999 Abandoned ----Ecology
29 1 29 SE SE RAY NOVAK 976800004 Domestic 87 87 6 77 87 30 3.25 44 0.074 10/9/1996 Sandstone ----Ecology & Jefferson
Co
29 1 29 SE SW BRIAN KILLMER 976800035 Domestic 85 85 6 65 85 14 7 62 0.113 8/27/1997 Basalt ----Ecology & Jefferson
Co
29 1 29 SE SW GEORGE LESLIE -Domestic 133 134 6 --15 ---3/30/1987 Basalt ----Ecology
29 1 29 SE JAMES BEEBE -Domestic 224 224 6 194 224 18 5 91 0.055 9/21/2005 Basalt ----Ecology
29 1 29 SE JIM BEEBE 976800041 Domestic 145 145 6 125 145 18 0.6 120 0.005 10/5/2004 Basalt ----Ecology
29 1 29 SW NE GENE HANSEN -Domestic 150 150 6 130 150 70 4 70 0.057 10/31/1991 Basalt ----Ecology
29 1 29 SW NE JOHN DALE -Domestic 80 80 6 60 80 19 3.5 --8/23/1991 Sandstone ----Ecology
29 1 29 SW NE MIKE PETERS 976800051 Domestic 67 67 6 47 67 11 2.5 52 0.048 10/10/1992 Basalt ----Ecology & Jefferson
Co
29 1 29 SW NE MORRIS SMITH -Domestic 88 88 6 68 88 20 3 65 0.046 7/25/1992 Basalt ----Ecology
29 1 29 SW SE ART JONES 976800056 Domestic 111 111 6 101 111 66 8 34 0.235 11/8/1998 Basalt ----Ecology & Jefferson
Co
29 1 29 SW SE DAVE WOODRUFF 976800038 Domestic 103 103 6 60 103 34 6 64 0.094 3/9/1988 Basalt G2-003115CL ---Ecology, Jefferson
Co, 2005 WRATS
29 1 29 SW SE GARY GRISWALD 995700001 Domestic 118 118 6 --18 10 90 0.111 10/4/1995 Basalt ----Ecology & Jefferson
Co
29 1 29 SW SE JIM COOK 976800036 Domestic 104 104 6 84 104 34 8 55 0.145 9/2/1996 Basalt ----Ecology & Jefferson
Co
RECEIVED BY DCD 8/30/2022
!.
976800066
976800063
976800001
976800002
921292001
976800061
976800062
976800060
976800073
976800059
976800004
976800003
976800005
921292002
976800006
976800007
976800058 976800009
921292003
921292005
921292067
976800064
976800073
976800080
976800008
921292004921292045921292047
921292041
921292046
921292043921292042
921292003
921292005
976800057
µ
PROJECT NO.
FIGURE NO.
DATE:
DESIGNED BY:
DRAWN BY:
REVISED BY:
060115
1
June 2006
ACM
ACM
ACM
0 150 300Feet
!.Snider well
Parcels
T:
\
P
r
o
j
e
c
t
s
_
8
\
Site Location MapSnider Hydrogeologic AssessmentPort Hadlock, WA
RECEIVED BY DCD 8/30/2022
W :\060115 S nider W ell\U pdated 2014 R eport\P um p Test
Snider Well Step Test Data
Snider Pump Test
Port Hadlock, WA
Figure 2
0
200
400
600
800
1000
1200
1400
1600
1800
2000-2
0
2
4
6
8
10
12
14
16
18
-50 0 50 100 150 200 250 300 350 400 450
Ch
l
o
r
i
d
e
C
o
n
c
e
n
t
r
a
t
i
o
n
(
m
g
/
l
)
;
S
p
e
c
i
f
i
c
C
o
n
d
u
c
t
i
v
i
t
y
(
u
S
/
c
m
)
;
B
a
r
o
m
e
t
r
i
c
Pr
e
s
s
u
r
e
(
m
B
)
Dr
a
w
d
o
w
n
(
f
t
)
Elapsed Time (min)
Water Level Data Barometric Pressure
Specific Conductivity (uS/cm) - Field Specific Conductivity (uS/cm) - Lab
Chloride Concentration (mg/l) - Field Chloride Concentration (mg/l) - Lab
Ba
s
e
l
i
n
e
D
a
t
a
3 gpm Step
1 gpm Step
2 gpm Step
Re
c
o
v
e
r
y
D
a
t
a
RECEIVED BY DCD 8/30/2022
W :\060115 S nider W ell\U pdated 2014 R eport\P um p Test
Drawdown and Transmissivity
Calculation (1.0 gpm Step)
Snider Pump Test
Port Hadlock, WA
Figure 3
0
0.5
1
1.5
2
2.5
3
3.5
4
0.1 1 10 100 1000
Dr
a
w
d
o
w
n
(
f
t
)
Elapsed Time (min)
Water Level Data
Transmissivity CalculationAverage Pumping Rate = 0.92 gpm
ftgpds
QT /69538.0
)0.1(264
'
264 ==∆=
RECEIVED BY DCD 8/30/2022
W :\060115 S nider W ell\U pdated 2014 R eport\P um p Test
Drawdown and Transmissivity
Calculation (2.0 gpm Step)
Snider Pump Test
Port Hadlock, WA
Figure 4
0
1
2
3
4
5
6
7
8
9
10
0.1 1 10 100 1000
Dr
a
w
d
o
w
n
(
f
t
)
Elapsed Time (min)
Water Level Data
Transmissivity Calculation
Average Pumping Rate = 1.93 gpm
ftgpds
QT /21051.2
)0.2(264
'
264 ==∆=
RECEIVED BY DCD 8/30/2022
W :\060115 S nider W ell\U pdated 2014 R eport\P um p Test
Drawdown and Transmissivity
Calculation (3.0 gpm Step)
Snider Pump Test
Port Hadlock, WA
Figure 5
0
2
4
6
8
10
12
14
16
18
0.1 1 10 100 1000
Dr
a
w
d
o
w
n
(
f
t
)
Elapsed Time (min)
Water Level Data
Transmissivity Calculation
Average Pumping Rate = 2.93 gpm
ftgpds
QT /40297.1
)0.3(264
'
264 ==∆=
RECEIVED BY DCD 8/30/2022
ATTACHMENT 1
Water Well Reports
RECEIVED BY DCD 8/30/2022
RECEIVED BY DCD 8/30/2022
RECEIVED BY DCD 8/30/2022
RECEIVED BY DCD 8/30/2022
ATTACHMENT 2
Pump Test Data
RECEIVED BY DCD 8/30/2022
W:\060115 Snider Well\Field Data Reports Page 1 of 5
179 Madrone Lane North 811 First Avenue, Suite 480
Bainbridge Island, Washington 98110 Seattle, Washington 98104
(206) 780-9370 (206) 328-7443
Project:Snider Pump Test Project No.: 060115-001-01
Date:5/23/06
Pumping well:Snider Well
Well water level data collected from:TOC - North Edge
Water level measuring point:TOC - 1.07 ft AGS
Depth to initial static water level in feet:81.89
Clock Time
Elapsed
Time in
Minutes
Depth to
Water in
Feet
Drawdown
below Initial
SWL in
Feet
Pumping
Rate -
Flowmeter
(gpm)
Pumping
Rate -
Voumetric
(gpm)
Conductivity
(uS/cm)
Cl
(mg/l)Comments
5/23/06 7:43:00 -37.9 81.88
5/23/06 7:53:20 -27.6 Started logging.
5/23/06 8:00:00 -20.9 81.89 P-ducer set at 35.9909
5/23/06 8:10:00 -10.9 81.89
5/23/06 8:15:00 -5.9 81.9 0
5/23/06 8:21:00 0.1 Started Pump Test
5/23/06 8:21:30 0.6 0.97
5/23/06 8:23:10 2.2 1.04
5/23/06 8:23:50 2.9 0.93 869 173
5/23/06 8:26:30 5.6 83.96 2.06
5/23/06 8:28:00 7.1 0.71 Adjusted Flow
5/23/06 8:29:00 8.1 0.91
5/23/06 8:31:55 11.0 84.1 2.2
5/23/06 8:35:40 14.7 0.91 467.3 36
5/23/06 8:37:00 16.1 84.31 2.41
5/23/06 8:41:45 20.8 0.9
5/23/06 8:42:30 21.6 84.43 2.53 0.88
5/23/06 8:48:00 27.1 0.9 448.2 28
5/23/06 8:50:10 29.2 84.52 2.62
5/23/06 8:55:05 34.2 0.9
5/23/06 8:56:20 35.4 84.56 2.66
5/23/06 8:57:30 36.6 0.91 435.7 < 28
5/23/06 9:00:00 39.1 0.9 0.97
5/23/06 9:02:20 41.4 84.59 2.69 0.89
5/23/06 9:09:10 48.2 424.2 < 28
5/23/06 9:17:20 56.4 84.65 2.75 0.89
5/23/06 9:19:30 58.6 0.89 424.9
Notes:
Elapsed time and drawdown are based on a starting time of 5/23/06 8:20:55; the time at which the pump test was started.
Pressure transducer water level data was used for all plots and analyses.
PUMPING TEST DATA
RECEIVED BY DCD 8/30/2022
W:\060115 Snider Well\Field Data Reports Page 2 of 5
179 Madrone Lane North 811 First Avenue, Suite 480
Bainbridge Island, Washington 98110 Seattle, Washington 98104
(206) 780-9370 (206) 328-7443
Project:Snider Pump Test Project No.: 060115-001-01
Date:5/23/06
Pumping well:Snider Well
Well water level data collected from:TOC - North Edge
Water level measuring point:TOC - 1.07 ft AGS
Depth to initial static water level in feet:81.89
Clock Time
Elapsed
Time in
Minutes
Depth to
Water in
Feet
Drawdown
below Initial
SWL in
Feet
Pumping
Rate -
Flowmeter
(gpm)
Pumping
Rate -
Voumetric
(gpm)
Conductivity
(uS/cm)
Cl
(mg/l)Comments
5/23/06 9:28:20 67.4 84.67 2.77 0.89 434.1
5/23/06 9:44:10 83.2 0.9 451.4 28
5/23/06 9:46:00 85.1 84.72 2.82
5/23/06 9:51:15 90.3 0.83 0.76
5/23/06 9:54:05 93.2 0.82 463.9 28
5/23/06 10:00:05 99.2 0.89 468.8 Adjusted Flow
5/23/06 10:09:30 108.6 470.3 36
5/23/06 10:10:30 109.6 Collected Snider1 Sample
5/23/06 10:14:15 113.3 84.57 2.67
5/23/06 10:17:00 116.1 0.95 471.9 36
5/23/06 10:21:00 120.1 1.99
Started 2 gpm Step (Totalizer =
110 gal)
5/23/06 10:25:15 124.3 2.04
5/23/06 10:26:40 125.7 87.4 5.5 2.01
5/23/06 10:30:30 129.6 1.82 490.2 36
5/23/06 10:33:00 132.1 1.96 Adjusted Flow
5/23/06 10:33:50 132.9 88.5 6.6 1.96 1.8
5/23/06 10:38:30 137.6 88.87 6.97 1.94
5/23/06 10:40:30 139.6 1.93 515 41
5/23/06 10:44:35 143.7 89.08 7.18 1.93
5/23/06 10:50:40 149.7 2 1.88
5/23/06 10:56:10 155.2 89.52 7.62 1.99
5/23/06 10:59:50 158.9 1.59 Adjusted Flow
5/23/06 11:01:30 160.6 2.01
5/23/06 11:03:50 162.9 584 86
5/23/06 11:05:30 164.6 89.52 7.62 1.99
5/23/06 11:08:30 167.6 1.61 Adjusted Flow
5/23/06 11:09:30 168.6 1.98
Notes:
Elapsed time and drawdown are based on a starting time of 5/23/06 8:20:55; the time at which the pump test was started.
Pressure transducer water level data was used for all plots and analyses.
PUMPING TEST DATA
RECEIVED BY DCD 8/30/2022
W:\060115 Snider Well\Field Data Reports Page 3 of 5
179 Madrone Lane North 811 First Avenue, Suite 480
Bainbridge Island, Washington 98110 Seattle, Washington 98104
(206) 780-9370 (206) 328-7443
Project:Snider Pump Test Project No.: 060115-001-01
Date:5/23/06
Pumping well:Snider Well
Well water level data collected from:TOC - North Edge
Water level measuring point:TOC - 1.07 ft AGS
Depth to initial static water level in feet:81.89
Clock Time
Elapsed
Time in
Minutes
Depth to
Water in
Feet
Drawdown
below Initial
SWL in
Feet
Pumping
Rate -
Flowmeter
(gpm)
Pumping
Rate -
Voumetric
(gpm)
Conductivity
(uS/cm)
Cl
(mg/l)Comments
5/23/06 11:10:30 169.6 89.28 7.38 1.97
5/23/06 11:13:45 172.8 1.97 619 95
5/23/06 11:15:20 174.4 89.45 7.55
5/23/06 11:21:00 180.1 1.97 1.87
5/23/06 11:22:30 181.6 1.97 637 105
5/23/06 11:29:30 188.6 89.65 7.75 1.97
5/23/06 11:31:50 190.9 1.96 651 105
5/23/06 11:36:35 195.7 89.67 7.77 1.95
5/23/06 11:41:00 200.1 1.95 664 105
5/23/06 11:44:50 203.9 89.68 7.78 1.95 1.82
5/23/06 11:56:30 215.6 1.95
5/23/06 11:57:50 216.9 1.95 679 116
5/23/06 11:59:30 218.6 89.69 7.79
5/23/06 12:04:45 223.8 1.9
5/23/06 12:06:30 225.6 1.9 688 116
5/23/06 12:10:00 229.1 Collected Snider2 Sample
5/23/06 12:12:45 231.8 89.5 7.6
5/23/06 12:14:30 233.6 1.91 697 127
5/23/06 12:21:10 240.2 Start 3 gpm Step (Totalizer = 341.65 gal)
5/23/06 12:22:10 241.2 3
5/23/06 12:23:08 242.2 91 9.1 2.94
5/23/06 12:24:10 243.2 91.7 9.8 2.98
5/23/06 12:25:30 244.6 2.99 662 105
5/23/06 12:26:36 245.7 93 11.1 3.02
5/23/06 12:30:36 249.7 94.5 12.6 2.97 3.09
5/23/06 12:35:10 254.2 712 127
5/23/06 12:37:18 256.4 95.85 13.95 2.94 2.98
Notes:
Elapsed time and drawdown are based on a starting time of 5/23/06 8:20:55; the time at which the pump test was started.
Pressure transducer water level data was used for all plots and analyses.
PUMPING TEST DATA
RECEIVED BY DCD 8/30/2022
W:\060115 Snider Well\Field Data Reports Page 4 of 5
179 Madrone Lane North 811 First Avenue, Suite 480
Bainbridge Island, Washington 98110 Seattle, Washington 98104
(206) 780-9370 (206) 328-7443
Project:Snider Pump Test Project No.: 060115-001-01
Date:5/23/06
Pumping well:Snider Well
Well water level data collected from:TOC - North Edge
Water level measuring point:TOC - 1.07 ft AGS
Depth to initial static water level in feet:81.89
Clock Time
Elapsed
Time in
Minutes
Depth to
Water in
Feet
Drawdown
below Initial
SWL in
Feet
Pumping
Rate -
Flowmeter
(gpm)
Pumping
Rate -
Voumetric
(gpm)
Conductivity
(uS/cm)
Cl
(mg/l)Comments
5/23/06 12:44:10 263.2 2.96 718 116
5/23/06 12:49:20 268.4 96.75 14.85
5/23/06 12:53:00 272.1 96.97 15.07 2.93
5/23/06 12:55:00 274.1 2.92 742 138
5/23/06 13:05:00 284.1 759 151
5/23/06 13:07:05 286.2 97.32 15.42 2.92 2.98
5/23/06 13:14:30 293.6 783 151
5/23/06 13:16:45 295.8 97.46 15.56 2.92 3.01
5/23/06 13:23:40 302.7 795 151
5/23/06 13:26:50 305.9 97.61 15.71 2.94
5/23/06 13:33:10 312.2 814 164
5/23/06 13:36:05 315.2 97.68 15.78 2.93
5/23/06 13:42:20 321.4 828 164
5/23/06 13:45:30 324.6 97.69 15.79 2.91
5/23/06 14:03:20 342.4 854 164
5/23/06 14:04:25 343.5 97.76 15.86 2.92
5/23/06 14:14:00 353.1 97.74 15.84 2.9
5/23/06 14:17:50 356.9 873 178
5/23/06 14:20:15 359.3 97.65 15.75 2.84 Adjusted Flow
5/23/06 14:28:00 367.1 Collected Snider3 Sample
5/23/06 14:28:40 367.7 97.77 15.87 2.94 885 193
5/23/06 14:36:00 375.1
Stopped Pumping (Totalizer =
736.46 gal)
5/23/06 14:37:07 376.2 95.5 13.6 Monitored Recovery
5/23/06 14:37:49 376.9 94.5 12.6
5/23/06 14:38:13 377.3 93.5 11.6
5/23/06 14:38:30 377.6 93 11.1
5/23/06 14:38:51 377.9 92.5 10.6
Notes:
Elapsed time and drawdown are based on a starting time of 5/23/06 8:20:55; the time at which the pump test was started.
Pressure transducer water level data was used for all plots and analyses.
PUMPING TEST DATA
RECEIVED BY DCD 8/30/2022
W:\060115 Snider Well\Field Data Reports Page 5 of 5
179 Madrone Lane North 811 First Avenue, Suite 480
Bainbridge Island, Washington 98110 Seattle, Washington 98104
(206) 780-9370 (206) 328-7443
Project:Snider Pump Test Project No.: 060115-001-01
Date:5/23/06
Pumping well:Snider Well
Well water level data collected from:TOC - North Edge
Water level measuring point:TOC - 1.07 ft AGS
Depth to initial static water level in feet:81.89
Clock Time
Elapsed
Time in
Minutes
Depth to
Water in
Feet
Drawdown
below Initial
SWL in
Feet
Pumping
Rate -
Flowmeter
(gpm)
Pumping
Rate -
Voumetric
(gpm)
Conductivity
(uS/cm)
Cl
(mg/l)Comments
5/23/06 14:39:11 378.3 92 10.1
5/23/06 14:39:54 379.0 91 9.1
5/23/06 14:40:17 379.4 90.5 8.6
5/23/06 14:40:43 379.8 90 8.1
5/23/06 14:41:38 380.7 89 7.1
5/23/06 14:42:41 381.8 88 6.1
5/23/06 14:43:57 383.0 87 5.1
5/23/06 14:45:37 384.7 86 4.1
5/23/06 15:06:20 405.4 83.1 1.2
Notes:
Elapsed time and drawdown are based on a starting time of 5/23/06 8:20:55; the time at which the pump test was started.
Pressure transducer water level data was used for all plots and analyses.
PUMPING TEST DATA
RECEIVED BY DCD 8/30/2022
ATTACHMENT 3
Water Quality Reports
RECEIVED BY DCD 8/30/2022
RECEIVED BY DCD 8/30/2022
RECEIVED BY DCD 8/30/2022
RECEIVED BY DCD 8/30/2022
ATTACHMENT 4
Wa ter Conservation Measures
RECEIVED BY DCD 8/30/2022
RECEIVED BY DCD 8/30/2022